Journal of Membrane Science 346 (2010) 8–14
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Journal of Membrane Science
journal homepage: www.elsevier.com/locate/memsci
Development of novel backwash cleaning technique for reverse osmosis in
reclamation of secondary effluent
Jian-Jun Qin
a,∗
, Maung Htun Oo
a
, Kiran A. Kekre
a
, Boris Liberman
b
a
The Centre for Advanced Water Technology, PUB Consultants Pte Ltd, Singapore 608575, Singapore
b
IDE Technologies Ltd, Israel
article info
Article history:
Received 3 May 2009
Received in revised form 16 July 2009
Accepted 5 August 2009
Available online 11 August 2009
Keywords:
Reverse osmosis
Backwash cleaning
Direct osmosis
High salinity
Water reclamation
abstract
The objective of the study was to further develop a novel cleaning technique for reverse osmosis in
reclamation of municipal secondary effluent. This technique is a new backwash method via direct osmosis
(DO) by intermittent injection of the high salinity (HS) solution without stopping of high pressure pump
and it is environment and membrane friendly technique. In the study, DO-HS trials were carried out with
a UF-RO pilot system which was operated on site with the secondary treated effluent as the raw feed.
Different operating conditions for DO-HS treatment in the actual process were investigated. It was found
that the operation for implementation of the DO-HS cleaning technique developed was easy. For the
first time, the actual profiles of HS concentration, DO backwash flow rate, brine flow rate and permeate
pressure during DO-HS treatment have been demonstrated. It was observed that turbidity of the brine
stream during DO-HS treatment at 3 NTU was 5 times higher than that before DO-HS treatment. The
results from this study have confirmed the previous hypothesis with DO-HS treatment that there would
be a strong driving force for DO backwash to lift and sweep the foulants from the membrane surface
which would be carried over to the brine. The optimal plant operating conditions in terms of RO feed
flow rate, HS concentration and HS injection time are ready for the DO-HS method to be adopted and
validated in a long-term continuous plant operation.
© 2009 Elsevier B.V. All rights reserved.
1. Introduction
Reverse osmosis (RO) is a pressure driven membrane process
and has been widely applied in various water treatment processes
as a promising technology [1]. However, RO membrane fouling is a
global issue. RO fouling is usually classified into four major types:
colloidal fouling, organic fouling, inorganic fouling/scaling and bio-
fouling. Hong and Elimelech [2] have reviewed the common fouling
factors, typical preventive strategies and their effective results that
have been explored in most studies. Of which, chemical cleaning
is most widely used to control membrane fouling and maintain
the membrane performance [3] although physical cleaning such
as forward/reverse flushing and air sparging is effective for specific
fouling [4]. However, these approaches will cause low effectiveness
of production due to the downtime of frequent RO operation stop-
page and create environmental issues related to the waste chemical
disposal.
Engineered applications of FO/DO in membrane separation
processes have been extensively reviewed by Cath et al. [5]
and Cornelissen et al. [6] and will not be discussed in this
∗
Corresponding author Tel.: +65 63262914; fax: +65 63262929.
E-mail address: QIN Jianjun@pub.gov.sg (J.-J. Qin).
paper. Development of forward osmosis (FO) or DO technology
has been increasingly attractive for backwash cleaning of RO
as it is highly efficient and environmentally friendly technique
[7–18].
Spiegler and Macleish [7] investigated DO backwash of RO mem-
branes about 30 years ago. That time, knowledge on DO backwash
under realistic plant operating conditions was scarce although it
was in practice known that periodic release of the brine pressure
of a RO plant could create a forward flush and temporarily recover
production rate which had gradually reduced in the course of the
plant operation. In their lab scale studies, an osmosis technique
was developed to clean and possibly to backwash contaminated
cellulose acetate RO membranes. They found that the RO flux
could be restored after DO backwash although the RO membranes
were fouled with ferric hydroxide and performed significant flux
decrease. However, it daily took at least 30 min for each operation
of osmotic backwash.
Ando et al. [8,9] invented a backwash method and treatment
system for spiral wound membrane modules and employed a per-
meate back pressure in the range of 0.05–0.3 MPa for backwash of
a spiral wound RO membrane module. Rychen et al. [10] reported
a new DO backwash process and device for producing pure water
with RO and no pressure was supplied at the permeate side. In
that method, the RO production process was stopped when the
0376-7388/$ – see front matter © 2009 Elsevier B.V. All rights reserved.
doi:10.1016/j.memsci.2009.08.011